My bad for the delay, but I wasn't able to take her for a spin until after work today.
So the first thing I did was modify this piece, let's call it (A). This piece secures the folding mechanism into the buffer tube threads on the JR Carbine.
Couple issues here.:
- The portion of the JRC that accepts the buffer tube seemed too shallow for the above piece, so the folding mechanism was not secure when installed.
- This buffer tube threads in JRC aren't threaded all the way to the stop, so the threads of (A) bottom out before they need to.
My fix was twofold.
- As shown in the picture above, I filed the bottom of (A) to shorten it so as to snug up the folding mechanism.
- I used a smaller file and a table vise to turn the front portion of (A)s threads down. This prevented the threads from bottoming out and let me snug (A) securely in the JRC. I did not turn all the threads down, on the first ring or so.
The next picture shows this completed step.
With this portion out of the way, next I was on to the bolt extension.
If you didn't already know, the Law Tactical folder uses this bolt extention, let's call it (B), to compensate for the added length of the folding mechanism. Normally, this extension fits inside a standard AR15 bolt carrier and is secured when you tighten down the internal screw, which pushes the metal prongs (shown in the picture below) out and secures the piece inside the bolt carrier. The JRC, on the other hand, uses a totally proprietary bolt and bolt carrier that is much smaller in diameter and makes the original attachment system impossible to use.
My solution:
- Remove screw and ball bearing from (B), keep the screw!
- Place (B) in vise as shown above and cut off prongs with a hacksaw.
With this done I test fit (B) in the JRC with bolt and folding mechanism installed. The goal here is to be able to get the spring loaded bolt stop on the Law Tactical folder to snap over the lips on (B). Sounds confusing, but if you have one in front of you it should make sense. Unfortunately, even with the prongs cut off (B) was much too long to fit.
My solution:
- Take (B) to my table mounted grinder and grind away on the end that I had cut the prongs off to get desired length.
- Continuously test fit (B) in the JRC until I was close enough to use a hand file.
- Place (B) in table vise and carefully use a file to evenly finish end of (B) until I had a nice flat and square surface.
With this accomplished, I threaded the screw from before back into (B) so that it looked like the picture below.
For the final step I had to seek out a local machine shop. My idea was to drill and tap the JRC bolt extension, let's call it (C), so that I could then just screw (B) as shown above into (C). Where as I killed my home drill press and ruined the original (C) on my own, my local shop easily drilled and tapped the new (C) that I had had shipped to me.
The only issue was to time (B) into (C), so that (B) would clear the buffer retainer pin. The result, you can see next!
Now when all was said and done, I cold-blued all the parts I had worked on and applied locktite where needed. Everything is nice and solid, and I can happily say that after 133 (suppressed) rounds fired earlier tonight, I didn't have a single malfunction and everything remained totally solid and secure. Now I can fold the stock for storage or travel, and it's much less of a hassle to remove the bolt to clean.
As always, your results may vary, and I can't advise you nor do I take responsibility for any actions you or others may take in relation to this post.