I used a mat. The heat transferred far enough maybe not to the point of getting burnt but uncomfortable. I put in a shop vac hose on the floor to keep fumes down. Ground connected to boat. I tried the ground in various locations but it didn't seem to matter, max distance was maybe 10'.
I'd originally tried to fill one hole with some of that aluminum brazing rod. It didn't really "wet" to my satisfaction so I ground as much as I could off and welded it. Made an arcing/burning mess until it was burned away by the plasma.
I did many coupons to try to get proficient but table top is different than awkward positions. I'm embarrassed to show my work since much of it looks like crap but I did improve a lot. Most difficult part for me was that the lap (faying?) joints layers would always distort and pull away at the slightest amount of heat. Nothing to use to clamp or hold that I could come up with easily.
Basically an aluminum drift boat that had 90 degree angle extrusion welded over the bottom to side joint. That extrusion was worn to knife edge thin. It was cut along the bottom at 6" intervals to allow it to curve. I tacked it at first where I could best get it to fit then hammered it to fit and tacked every 6" at the cuts. Ultimately decided to tack every 3" and finally fill between every fourth set of tacks.
I had probably about 15 pinhole burn throughs that I had to hit from the inside. Probably will find more when I put it in the water hopefully tomorrow.
Steelhead was closed to fishing from boats in much of WA this year so I didn't lose much. Decided I'm going to use Wetlander instead of Gluvit for the bottom coat.
ETA: .080" aluminum. Probably the original metal was 6000 series. The replacement angle was 5000 series the one that's OK to use 4043 rod on. 4043 seemed to wet better than 5036 (?) not sure if that's the number. Turned to balance up to more like 40%, seemed to work better with this old aluminum.